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This study assessed the technical feasibility of removing nitrogen from municipal wastewater by partial nitrification (nitritation) in a continuous plug-flow step feed process. Nitrite in the effluent accumulated to over 81.5 +/- 9.2% but disappeared with the transition of process operation from anoxic/oxic mode to the anaerobic/anoxic/oxic mode. Batch tests showed obvious ammonia oxidizing bacteria (AOB) stimulation (advanced ammonia oxidation rate) and nitrite (NOB) oxidizing bacteria inhibition (reduced nitrite oxidation rate) under transient anoxic conditions. Two main factors contributed to nitritation in this continuous plug-flow process: One was the alternating anoxic and oxic operational condition; the step feed strategy guaranteed timely denitrification in anoxic zones, allowing a reduction in energy supply (nitrite) to NOB. Fluorescence in Situ Hybridization and quantitative real-time polymerase chain reaction analysis indicated that NOB population gradually decreased to 1.0 +/- 0.1% of the total bacterial population (dominant Nitrospira spp., 1.55 x 10(9) copies/L) while AOB increased approximately two-fold (7.4 +/- 0.9%, 1.25 x 10(10) copies/L) during the above anoxic to anaerobic transition. Most importantly, without addition of external carbon sources, the above wastewater treatment process reached 86.0 +/- 4.2% of total nitrogen (TN) removal with only 7.23 +/- 2.31 mg/L of TN in the effluent, which met the discharge requirements. (C) 2014 Elsevier Ltd. All rights reserved.
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来源 :
WATER RESEARCH
ISSN: 0043-1354
年份: 2014
卷: 55
页码: 95-105
1 2 . 8 0 0
JCR@2022
ESI学科: ENVIRONMENT/ECOLOGY;
ESI高被引阀值:309
JCR分区:1
中科院分区:1